So, I'm nearly there with the floor - got the inside finished anyway
For some reason it looks patchy in the photos - doesn't in reality but it's going under the carpet anyway.
Then I got some 3M PU seam sealer in a tube, beaded this down the seams and brushed them out to give the 'Ford' look.
Looks all dusty :roll: I must have hoovered this car nearly 10 times during this process! :lol:
Used Thermotec heat tape to cover parts close to the down pipe..
Finally got my turbo and down pipe back in
Then I set about mounting the airbag module again. Surprisingly, this turned out better than I'd expected.
Then neatened up, painted and re-fitted. This is really sturdy believe it or not! The thing is like rock, which is how I wanted it and how it needed to be given that I think it's mounted directly to the floor for a reason.
And wiring tucked in, close, but not too tight. I put some rubber trim on the support for the dash anyway.
Made up this little bracket to support a water hose and oil drain from turbo near the crank position sensor.
Meanwhile, someone decided to bump our Leon and leave without a care in the world:
I then realised I had a slight fouling on my subframe and a CV boot which resulted in re-jigging it slightly. As I mentioned previously I think I'll be getting another one next year and re-doing the bits I've modded a bit better and get the whole thing powder-coated.
Replaced heater control panel with a non A/C version. A little scratched, but it will do for now - I hope it works as I've been having trouble with it all.
I think that's all! I also went to get it ready for starting Friday night and found I couldn't get any oil pressure. Eventually I found out that because the engine has been sitting there so long, the oil pump had become very dry and was just spinning in air and not creating any suction. So I back filled the oil line to the pump and checked it pumped back up which it did. Saturday I made sure I goot 40 psi pressure just from cranking it on the starter. I then coonnected ECU, ignition and I could hear a fuel leak. Feed O ring for the rail had split so replaced that. Then finally early evening on Saturday started her up.. a few seconds crank and she was away. Sounded a little rough on idle as I haven't sorted the VSS yet... but very pleased, it's been a long time coming!